More problems, LOL! We didn't get to run the Guiness 1/4 mile race. We had the sled already to go, made an early 1000' pass right away to make sure all was good, air was perfect and about -0- degrees out, BUT, the sled took off extremely quick with Glenn Hall riding and without a doubt was going to be a very fast pass, then "POP" at 1/2 track. The turbo overboosted to its limits of 45+ psi of boost, due to the cold air and exhaust size turbo housing (thats why it looked so fast) and stretched the head studs, leaking boost pressure into the coolant system and blew off the coolant lines and blewout the crank seals on recoil side.
Soooo.... today I'm tearing down the engine and machining crank seal retainer plates and beefing up the head studs. The sled should be ready to go by next Sunday night. Sucks, but thats racing and this is what it takes to get to the next level with these crazy horsepower levels...More horsepower, more problems. We'll be ready for Forest Lake in 2-weeks with an even stronger fresh Vmax-4 engine.
Take care guys...I better go get busy!!!